Thanks to Grayson Ottoway who has sent in this post recounting the crash of Lockheed Electra AK-AGK 65 years ago today..
On the morning of 23 October 1948 two experienced pilots, Commander
Max Hare and Second Officer Brian Russell, flew ZK-AGK Kaka, a Lockheed Electra
of the National Airways Corporation’s fleet, from Hamilton to Palmerston North. They were due
to make the return journey later that day.
At 1.16 p.m., after refuelling and taking on board 11 passengers,
Kaka took off towards Whanganui. This ‘dog leg' added time and distance, but
kept airliners clear of the peaks of Ruapehu, Tongariro and Ngāuruhoe at a safe
cruising altitude, in an area where navigation beacons were scarce. Kaka
initially appeared to be on course: it reported its presence at the Whanganui
beacon at 1.38 p.m, when it was flying in heavy cloud and rain, and was later
seen overhead at Ōhakune. Fears began to be held for the safety of the crew and
passengers when it failed to report its position 30 minutes north of Whanganui,
and did not arrive in Hamilton
as expected.
An intensive aerial search ensued. Numerous military and civil
aircraft searched each day until the light failed or they were stopped by bad
weather. But with hundreds of residents reporting to have heard aircraft in
trouble, their efforts were dispersed across the centre of the North Island . A breakthrough finally came when three
deerstalkers came out of a densely wooded area on the western side of Mt
Ruapehu. They said they had heard an aircraft’s engines cut out near the
mountain on the day Kaka went missing. Eventually wreckage approximately 900 m
from the summit of the mountain was detected from the air.
Search parties left for the site on the morning of 29 October. Little
hope was held of finding anyone alive – weather conditions on the mountain had
been poor and almost a week had passed since Kaka had disappeared. When the
searchers arrived the following day, all 13 passengers and crew were found to
have been killed on impact. The bodies were recovered, wrapped in blankets and
parachute material, and carried down the mountain to Horopito.
The board of inquiry into the crash concluded that the aircraft had
gone off course because the pilot had made an error in his calculations, but
also suggested that the lack of navigation beacons in the central North Island was a contributing factor.
Influenced by this, the fifth
major fatal accident in 11 years, late in 1948 a government commission
recommended restructuring civil aviation and the need for industry regulation –
including more rigorous in-flight safety procedures for commercial pilots.
Photo : Ed Coates Collection |
No comments:
Post a Comment